Spaceclam
Cruisin' Guzzisti
So on sunday, i decided to try and measure my squish clearance, as per the recomendations of many. It turns out the bolt that is recessed behind the inner spark plug has a stripped head (from the factory) and can not be removed, but that's not the strange development.
I started with the left side, because i could do it without taking the tank off. Before i went around loosening any bolts, (yes, i did them all in a star pattern, or rather started to) i measured my valves at 5 and 7. (i set them at 6 and 8 about 4k miles ago, but the bike is still new) Also, my exhaust valve was stark white, and had the texture of having been sandblasted. I haven ever seen this before. roughly 6200 miles. :?:
After LOOSTENING but not removing the bolts in a star pattern, the stripped bolt was the last, by coincidence. so having already untorqued things, i just decided to re-torque things, put the project off for another time, and put stuff back together.
I reset my valves back where they were before the aborted surgery, at 5 and 7. They werent too far off, but having untorqued the heads and jugs, i figured i should probably do it anyway.
MY BIKE PINGS A LOT LESS. I dont know why, i didnt change anything. At first i thought it was the weather, but it warmed up today, and i did about 5 consecutive full throttle pulls up a rather steep incline in 5th gear, through my pinging range, 4-5k. I'd still like to tweak the timing a little bit, but THIS i could live with if i had to.
I have no explanation for this. I didnt change anything :huh:
I started with the left side, because i could do it without taking the tank off. Before i went around loosening any bolts, (yes, i did them all in a star pattern, or rather started to) i measured my valves at 5 and 7. (i set them at 6 and 8 about 4k miles ago, but the bike is still new) Also, my exhaust valve was stark white, and had the texture of having been sandblasted. I haven ever seen this before. roughly 6200 miles. :?:
After LOOSTENING but not removing the bolts in a star pattern, the stripped bolt was the last, by coincidence. so having already untorqued things, i just decided to re-torque things, put the project off for another time, and put stuff back together.
I reset my valves back where they were before the aborted surgery, at 5 and 7. They werent too far off, but having untorqued the heads and jugs, i figured i should probably do it anyway.
MY BIKE PINGS A LOT LESS. I dont know why, i didnt change anything. At first i thought it was the weather, but it warmed up today, and i did about 5 consecutive full throttle pulls up a rather steep incline in 5th gear, through my pinging range, 4-5k. I'd still like to tweak the timing a little bit, but THIS i could live with if i had to.
I have no explanation for this. I didnt change anything :huh: